Some Surge Investigations on a Low Speed Compressor

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dc.contributor.author R.C. Turner en_US
dc.contributor.author R.A. Burrows en_US
dc.date.accessioned 2014-10-20T11:02:44Z
dc.date.available 2014-10-20T11:02:44Z
dc.date.issued 1961 en_US
dc.identifier.other ARC/CP-548 en_US
dc.identifier.uri https://reports.aerade.cranfield.ac.uk/handle/1826.2/561
dc.description.abstract This paper summarises some exploratory tests on a low speed low pressure ratio multi-stage axial compressor, in which mismatching was simulated by appropriate staggering of the stages, the last stage alone being unchanged. Overall and stage characteristics and surge flow coefficients were determined for two degrees of mismatching and for the fully matched condition. In addition, velocity and yaw traverses were made at the first and last stages, and flow fluctuation measurements were also made at selected positions. en_US
dc.relation.ispartofseries Aeronautical Research Council Current Papers en_US
dc.title Some Surge Investigations on a Low Speed Compressor en_US


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